Monte Carlo

We have a WHAT?

Posted in MDX, Maxima, Monte Carlo on December 28th, 2008 by Aren Cambre – Be the first to comment

In August, my ‘97 Chevrolet Monte Carlo waned my fiscal conservatism. I must have looked at it wrong, as it came down with more problems. I already hate that car, a pathetic product of a union-starved, incompetently led corporation. It may have needed another intake manifold gasket replacement, more A/C work, and possible oil and crankshaft seal replacements.

Plus, kid #2 on the way is a convenient excuse…

You’ll be amazed: I don’t like SUVs. But now we have one. Here’s the logic:

Luggage taken on a 2 week trip with a 1 year old boy.

Luggage taken on a 2 week trip with a 1 year old boy.

  1. Wife wanted a larger vehicle but hates minivans. I’m OK with the “larger vehicle” part. The stuff pictured at right is everything we brought on a 2 week trip when our son was 1 year old. Yes, it fit in our ‘02 Nissan Maxima, but barely. I can’t fathom how we could pack for 2 kids. We went back and forth on the minivan vs. SUV argument, but the SUV won both because of spousal preference and…
  2. Used SUVs are cheap! The price savings alone pays for several years worth of additional of gas.

After research and a few test drives, we focused on the 2006-2007 Honda Pilot. We didn’t go earlier than 2006 because only 4×4 models were available.

The dealers are idiots. None seemed to know how little their SUVs are worth. The “no pressure” dealers had exorbitant, barely-negotiable pricing. All of them lie, lie, lie.

2 weeks into the search, we checked the Acura MDX. While it’s the Pilot’s corporate cousin, it’s not the same sense as GM’s chicanery, where they took an Oldsmobile 98, tweaked the outside, slapped on leather seats and other doo-dads, and called it a Cadillac Fleetwood.

To our shock, Autotrader’s MDXes listed for less than the Pilot! HUH?

After a test drive and a couple more days of looking, Jennifer found a MDX for sale by a private owner. Pictures looked great, a VIN search checked out, etc.

Long story short, we met the guy on Monday, had it inspected, and by Thursday we were at his credit union buying it from him.

So here’s the new Cambre garage mate:

I still cannot believe that these are cheaper than Pilots, and I cannot believe the deal we got.

A while back, I told my wife I would never want a “luxury car.” It just didn’t feel right. Well, we have one now. It still doesn’t feel right, but the price was right!

I hate my car

Posted in Monte Carlo, Nova on December 22nd, 2007 by Aren Cambre – 2 Comments


I have a hate/hate relationship with my 1997 Chevrolet Monte Carlo.

It’s a former rental car, purchased for my wife in early 1998 from Hertz Car Sales with only 14,000 miles.

It became my “hand me down” in 2004 when we got my wife a 2002 Nissan Maxima after I wrecked my 1974 Chevrolet Nova.

This Monte Carlo has no character. I gives me no pride. It does little more than semi-reliably go to and from work.

Since 1998, this car has had all these problems:

  • Gasket failure on high side A/C service port
  • A/C compressor electrical feed failure
  • Oil leaks everywhere (oil regularly changed)
  • Noisy timing chain rattle when engine is cold
  • Major intake manifold gasket coolant leak (yes, the coolant was changed before the regular service interval due to the next problem…)
  • Water pump leak
  • Master cylinder leak ($550 dealer only job)
  • EGR failure (twice)
  • Two alternator failures
  • Heater core failure
  • Radiator failure
  • Heater bypass line failure (both lines)
  • Gas regulator leak
  • Flaky 4th gear torque converter clutch (trans fluid changed per manufacturer’s schedule)
  • Driver’s side power window that doesn’t go up correctly without assistance
  • Poorly fitting dash parts
  • Cheap interior parts that break when a heavy guy leans on them (car was not even 2 years old at the time)
  • Rearview mirror fell off
  • Disentigrated controls on passenger’s A/C vent
  • Handling worse than a Toyota Corolla
  • 3.1L that only has 160 HP (!) and doesn’t do better than 24 MPG at 70 MPH

Despite all this, in an objective comparison with my Nova, it would win hands down except in the horsepower department. But my Nova had character and history. It was part of my self-identity, and it was my automotive passion.

This Monte Carlo is mediocrity. It was mediocre in 1997. Today it’s less than mediocre. It’s a token child of GM’s multi-decade malaise.

With my Nova, I wanted to fix everything. I’m embarrassed at how much I spent on it.

With the Monte Carlo, I don’t care. As long as it’s comfortable and safe, I don’t care. I don’t care that the SERVICE ENGINE SOON light has been on for months (it’s the EGR). I don’t care that the suspension is getting bouncy. I probably need to rotate the tires, but I don’t care. I haven’t washed it in 2 years.

I just don’t care.

Here’s where I am conflicted. This car almost always completely satisfies my transportation needs. It gets me where I want to go. It’s holding up better than some of my coworkers’ similarly-aged SUVs with fewer miles. It’s saving me a ton of money, especially compared to new car depreciation.

Why do I dislike something that does exactly what I need?

I’ve thought about this, and I may still be struggling with how I relate to cars. I used to have a car that was like an extension of me, of my personality, something I could take pride in. It was involuntarily taken away from me, and now this mediocre substitute is all I have.

I’m lusting after the 2006 Pontiac GTO (has to be manual transmission) and 2007 Honda Civic Si 4 door. But I know I cannot buy a passion. All they would represent is a poor financial choice: appreciating assets (investments) turned into depreciating assets (cars).

Oh, well. At least I can have “pride” in one thing: I practice the fiscal conservatism I preach.

Shrug.

Radiator replacement post-event fun

Posted in Monte Carlo on December 22nd, 2007 by Aren Cambre – Be the first to comment

Even after replacing my Monte Carlo’s radiator two Saturdays ago, my cooling system still gave me trouble!

On the following Tuesday, a small coolant bypass line, which provides hot water to the intake manifold, split open, creating a smoking engine compartment and a nauseating smell of scorched coolant. I managed an emergency bypass line replacement that evening despite rain and a Boy Scout Commissioner Staff meeting.

If that wasn’t enough, my upper radiator hose cracked open 9 days later. This hose was all of 3½ years old (replaced during intake manifold replacement gasket event)! Does that say something about parts store hoses?

Fortunately, replacement was simple, especially thanks to a coworker letting me borrow a socket wrench set. (Why did I not have one in the car with me?) After an emergency hose replacement in the SMU parking garage, I hope the car is finally sealed up!

Radiator replacement

Posted in Monte Carlo on December 8th, 2007 by Aren Cambre – 1 Comment

I replaced my Monte Carlo’s radiator today. The job wasn’t as bad as I thought it would be.

This leak started a couple of weeks before Thanksgiving. Before realizing it was an unfixable leak where the plastic side tanks met the metal center part of the radiator, I ran a can of stop leak in the system in a futile effort to make it last longer. It didn’t work, and it lately got to the point where I was refilling the reservoir every other day.

I had to do this today (Saturday, Dec. 8) because the weather is turning cold and rainy tomorrow (Sunday, Dec. 9).

Here’s how I started out:

45 minutes later, it’s out. Here’s the condenser:

The old radiator and the new one on the box:

I had to take some clips and parts off the old one and put it in the new one. One of the parts was the coolant level sensor. It was full of “mud”:

This “mud” is apparently common in systems running GM’s orange Dexcool coolant. As an aside, this coolant is commonly blamed for many problems. My gut feeling is that Dexcool’s faults are badly overblown, and at worst, may be responsible for a small increase in problems only with certain vehicles–such as 3.1L engines eating intake manifold gaskets (part 1, part 2)!

The new radiator is installed, and all parts are back in place:

I saw this notch in the radiator:

It turns out it only dug into the fins, not the tubes, and the old radiator had it, too. I guess it allows the radiator to flex laterally? While aluminum allows for far more efficient radiator design, it is more rigid and less bend-tolerant than older brass radiators.

Refilling the radiator in these cars involves opening some bleeder screws in the engine. I think it is this way because, due to the aerodynamic shape of the front of the car, the top of the radiator is well below the intake manifold. Therefore, you have to open the bleeders while filling and again while the engine is running to let air bubbles escape. Otherwise, the thermostat may take a while to open.

The car is back together, and the leak is gone!

A/C Fun, Part 4

Posted in Monte Carlo on June 3rd, 2007 by Aren Cambre – Be the first to comment

(This is continuing from where I left off.)

I got a replacement high side port valve and compressor oil. Here is the valve:
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The old one came right out:
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Once installed, the new port one looks like the old one, so I won’t bother you with another picture.

After flushing and adding new oil to the vacuum pump, I ran into another hiccup: the pump had a 1/4″ male flare fitting, but my R-134a gauge and hose set appears to have a 5/16″ female flare fitting. Argh! A last minute trip to Home Depot taught me that 5/16″ flare fittings are unusual.

Coming home defeated, I remembered that I had an extra high side service port for a R-134a retrofit. This was left over from my Nova. Luckily, it fit the vacuum pump!
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This is a weird arrangement, but it works. I pump through the red hose instead of the yellow hose. The yellow hose was hooked up to a can tap on a R-134a can.

That vacuum pump is awesome. It sucked down to an indicated 31 in/Hg in a hurry:
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I doubt that was really 31 in/Hg. I’ll bet the gauge set is actually off a bit.

Here was the whole setup:
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I closed off the gauges for the leak down test. In about 15 minutes, the needle crept to around 27 in/Hg. Normally that is a bad sign; if your system is properly sealed, the vacuum won’t budge a bit. However, I didn’t have a high side port cap installed, and I wasn’t totally confident in the low side hose’s attachment to the low side port. Plus, it was getting late, I had a 9:00 AM meeting the next morning, and I needed to make something happen. So I just let that small loss be a passing grade, figuring I could check it later and hoping the leak was because of the auxiliary issues and not an actual system leak.

Factory spec for my car is 30 oz of R-134a. I sucked down two 12 oz cans, bringing me to 24 oz. But what do I do about the remaining 6 ounces?

Professional refrigerant charging equipment uses a large gas cylinder, similar to propane grill cylinders, that’s on a scale. As the car’s A/C sucks in refrigerant, the scale measures the change in weight of the cylinder.

I realized I could do the same at home:
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That’s a can of R-134a sitting on a kitchen ounce scale! It worked great.

I checked my pressures over the next few weeks, and they held fine, strongly suggesting the new high side port solved the entire refrigerant leak.

But here’s the problem: the A/C didn’t feel as cool as before, especially when at a stop. The vent temperatures “felt” OK, but the car’s interior just didn’t feel the same. And it wasn’t that humid, system undercharge feeling, either.

Each time I checked the pressures, the ambient temperature was in the mid-80s. The low side pressure was just below 30, and the high side pressure was around 250. Those seem like OK pressures, so what gives?

Consulting with a guy who does a lot of A/C work, he suggested I shoot a few more ounces of refrigerant in the system. I put in the remaining 6 ounces from that half-used can, and the cooling only got a little worse. Checking pressures, the high side stayed around 250 or so, but the low side never got below the low 30s.

Today, I recaptured some of that extra refrigerant with my homemade refrigerant recovery system!
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Yup, that’s the empty R-134a can on an ounce scale to the side:
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I never disconnected it from the hose set. And it actually would not be empty; it would still have at least 30 or so PSI of R-134a in it because there is no way a full system would suck it down more.

The plan was to gradually open the high side valve on the gauge set until the can had 12 oz or the low side reading got to the mid-20s. I hit both markers at about the same time. Surprisingly, even with a theoretical 6 oz undercharge, the system still did a 250 PSI on the high side!

Here’s the high tech device I use to keep the engine RPMs up during A/C diagnostic operations:
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Here’s the gauge reading after removing all 12 ounces:
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I don’t get it.

Over the last few weeks, I was complaining to a couple of people about my vent temperatures. Turns out that my thermometer was reading 5-6 degrees too high. The black-needle thermometer is the one I was using, and the red-needle one is one of our kitchen thermometers:
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I later verified both thermometers against a verified digital thermometer in the house, and the red one is spot on.

It will be interesting to see how the system runs now with a theoretical 6 oz undercharge.

By the skin of my teeth

Posted in Aren, Monte Carlo, Traffic Safety on June 2nd, 2007 by Aren Cambre – 6 Comments

This morning, while driving on southbound Garland Road (TX 78) by White Rock Lake, I saw a careening, white Nissan Maxima headed the wrong way, barrelling down at me.

I could tell it was imminently going to swipe the Volvo wagon in front of me and was barrelling right at me from my left. So I jumped a curb and slammed on my brakes.

I ended up halfway on grass and halfway on a hike and bike trail:
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(All pictures are from my cell phone and have poor color balance.)

Luckily, no runners were in my path! I took longer than the Volvo to stop because the grass was wet with dew. Thank God for antilock braking!

If you look closely, you’ll see a Toyota Highlander about 100 feet in front of me. It also had to jump the curb. I guess the lady in the Volvo wasn’t paying good attention; she could have avoided the crash if she got off the road, although I may have then run into her?

Here’s where I launched off the curb:
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One of my left wheels did that.

I barely missed the careening Maxima.

Once I realized I was OK, I jumped out of my car and checked on the lady in the Volvo. She was dazed and just wanted out of her car. She couldn’t open her driver’s door:
image_00040.jpg

Seeing that no immediate action was needed, I called 911. I had to ask her twice to shut off her engine as I was on the phone; she was too startled to remember to do that.

Fortunately, she was totally unharmed. Her dogs were also startled and unharmed:
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The Maxima’s driver appeared to be in more trouble. As soon as I was comfortable that the Volvo lady was OK, I asked a bystander to help her with her dogs so she could get out. I then went to the Maxima.

The Maxima ended up doing a 180:
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Plenty of people were attending to the guy by the time I got to him. At first, I thought his head was bleeding, but it turns out the guy’s rasta-style dreadlocks were hanging over his shoulder. He was shaking and in apparent mild shock. Bystanders were reassuring him. Since he looked OK, I didn’t interfere. His passenger compartment was intact:
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He was complaining of foot pain. That wasn’t surprising given the impact location:

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Anyone need a coil spring?
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(It’s right in front of the car.)

I asked the guy in the green cap to wait for the ambulance and flag it down.

Based on the timestamps in the picture, I guess the fire truck didn’t arrive until about 5-6 minutes after the crash, and the ambulance was about 1 minute later. This surprised me since the fire station is just a mile away up the same road. But maybe that’s normal response time?

The paramedics got the guy on his feet, so I guess he was OK?
image_00059.jpg

The only cop to show up was a traffic cop (in Dallas PD, they wear red epaulets), and he arrived roughly 10-12 minutes after the crash. That response time shocked the heck out of me.

The crash appeared to be caused by an unobservant motorist who had to make a last minute lane change to avoid a slow-moving or stopped truck. The unobservant driver swerved into the Maxima’s path. In avoiding the unobservant driver, the Maxima’s driver lost control and careened into oncoming traffic.

Since I didn’t witness this part, the cop didn’t need me to stick around. After making sure the Volvo lady didn’t need more help (the emergency personnel weren’t helping her as she was unhurt), I took off for my meeting, which was about creating a foundation for White Rock Lake Park. Incidentally, my car ended up in this very park!

Do Volvos automatically blink headlights when the airbag goes off? I am not sure that a driver could make headlights blink:
image_00070.jpg

A/C Fun, Part 3

Posted in Monte Carlo on May 3rd, 2007 by Aren Cambre – 2 Comments

When I left off on this thread, I had fixed an electrical problem and buttoned up my A/C system, waiting to see if any leaks materialized.

The A/C ran decently on Monday, Tuesday, and Wednesday. In fact, Wednesday morning, the system dumped lots of condensation as I backed into a parking place. That’s a good sign.

Come Thursday, the compressor won’t kick on. Wiggling the clutch wire didn’t help.

After I put the kid to bed, I took a look. The high side service port cap looked off, so I checked it further and found it was broken. The center piece was still in the port:
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And notice all the green around the port? That’s the color of leak detection dye!

The plastic piece came out easily with a pocketknife.

I mixed up some soapy water:
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…and threw a little on the fitting and got bubbles:
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Eureka, I found a leak! The complete lack of visible dye anywhere else suggests this could be it!

The next question is how do I fix this leak? I have a Schrader valve repair kit, but there is some rubber piece over the valve that prevents me from engaging it:
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(This is looking straight down the valve.)

Looking two pictures up, you can see a clear hex pattern at the base of the service port. Does the port come apart? I’m going to check with a few people and figure this one out, hopefully soon!

Now here’s what I don’t get. I had enough refrigerant for the system to work acceptably on Monday, Tuesday, and Wednesday. Today, the pressure was almost 0 PSI:
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How did it lose so much refrigerant so quickly? Was the service port cover actually retarding the refrigerant flow, and it finally broke under pressure, allowing refrigerant to escape more quickly?

Stay tuned. Once I locate vacuum pump oil, I’ll get this completely fixed.

A/C Fun, Part 2

Posted in Monte Carlo on April 28th, 2007 by Aren Cambre – 1 Comment

Picking up from where I left off, I diagnosed that my ‘97 Chevrolet Monte Carlo’s compressor does not engage, and I suspected an electrical problem.

Yes, it was an electrical problem. But an easy one.

I had one trick to figure out. I need to test voltage at the compressor. Only problem is the power connection to the compressor clutch is frighteningly close to the electric radiator fan, and this fan comes on when I turn the A/C on.

I found the wiring diagram in my Haynes manual:
Compressor relay wiring diagram

It shows that the signal for the compressor passes through a relay, shown at right. Terminals 2 and 5 are always hot, powered by the same fuse. When terminal 1 is grounded, that closes the switch inside the relay, allowing terminal 3 to power something. In this case, when the powertrain control module grounds terminal 1, terminal 3 activates a diode on the compressor that engages the clutch. Here’s the terminals on the relay:
A/C relay
I pulled off the relay and found that the relay’s terminals 2 and 5 are hot even when the ignition is on the ON position, the engine is not running, and the A/C is off. That combination is important because I have power available to the compressor but I don’t risk danger from a running engine or a moving radiator fan.

I used a paper clip to short terminals 3 and 5, emulating what the relay would do if activated by the powertrain control module:
Shorting relay terminals

Then I pulled off the compressor clutch wire. It was really nasty, so I cleaned it up with carburetor cleaner:
A/C compressor clutch wire hanging loose

I tested for signal:
Testing compressor clutch wire
Eureka, the light came on! So I have compressor signal.

I also cleaned up the fitting on the compressor:
Compressor clutch connection

Plugging it back in, the compressor clutch clapped into place! But I also found that there is something flaky with the connection. If I move it wrong, the compressor disengages. I ended up finagling it into a position that works, but I’ll have to investigate that further later.

Now that I can turn on the compressor, I can properly charge the system. All told, I added about 20 oz of R-134a to the system. After doing that, I got these pressures at about 2000 or so RPM at 82 degrees ambient temperature:
Gauge reading (205/26)
That’s 205 PSI high and 26 PSI low. I think those were OK readings. I later found the static pressure to be 83 PSI, which corresponded to a 78 degree ambient temperature. I’m not sure how to interpret that since the actual temperatuer was about 4 degrees warmer.

But what bothered me more is when I came back to the car about 5 hours later, the static pressure dropped to 76 PSI. In retrospect, in those 5 hours, the National Weather Service recorded a 10 degree temperature drop at Love Field Airport, and the engine bay cooled down significantly. Those alone could fully explain the problem.

Still, doing my due diligence, turned off all the lights and got out my UV lamp and checked for leaks. For a reference point, I checked the UV overspill on the low side port where I injected it:
UV dye on service port
The dye puts off a clear yellow color.

I checked all around the compressor and fittings and lines and couldn’t find any evidence of dye:
Compressor in UV light

Seeing no leaks, I added a few more ounces of R-134a to the system and called it a day. I’ll check the system once again tomorrow to verify that it has plenty of refrigerant and button the system back up.

My plan for now is to just run it until I notice cooling problems. At that point, I’ll verify pressures again and check for leaks.

I do have one theory for why this all happened, although I think it is wishful thinking. My low pressure service port had no cap. It is theoretically possible that debris got in there and caused a slow leak.

Over the next couple of weeks, I’ll find out if that is the case.

A/C Fun, Part 1

Posted in Monte Carlo on April 28th, 2007 by Aren Cambre – 3 Comments

My ‘97 Chevrolet Monte Carlo’s A/C is dead, and I am going to fix it.

Last fall, towards the end of A/C season, the compressor got really noisy. I could really hear it at low speeds.

Come spring, the compressor won’t engage at all. This probably means a refrigerant leak, faulty compressor, or electrical problem.

You might say that a loud compressor automatically means it’s new compressor time. Not necessarily, says an A/C tech who specializes in GM vehicles: variable displacement V5 compressors can be noisy with too little refrigerant.

My first test is to check the refrigerant pressures. First step is to assemble the gauges:
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I tried to hook up the gauges, but I could only manage to get the high pressure side on. Here’s its reading:
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That’s not good at all. It’s indicating about 8 PSI, meaning I definitely have a refrigerant leak. I don’t recall exact normal idle pressures, but I am pretty sure it’s over 70 PSI.

I removed the air cleaner box to get good access to the low side fitting. This is looking straight down:
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Since I already knew I have a leak, I sprayed in some dye. This dye will help me find the leak later: the dye will appear near the leak point. If it doesn’t obviously show up in daylight, I will be able to detect the leak using a fluorescent “black light.” Here’s the dye can:
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You can see how bright the stuff is on the low side fitting:
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I got both sides of the gauges hooked up:
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I introduced enough R-134a to get the gauges to read about 63 PSI:
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I turned the car on and still got no compressor action.

Dang, that’s not good.

At this point, it appears to be an electrical failure. I’ve already gone through all the relays and fuses I am aware of: the fuses in the dash fusebox, and the relays on the front passenger side of the engine compartment. I swapped the relays and fuses out with identical neighboring ones and got nowhere.

I am going to consult with some people before I go on to the next step. However, it looks like I may be in for some “real fun” soon.

Intake manifold replacement DONE

Posted in Monte Carlo on April 5th, 2004 by Aren Cambre – Be the first to comment

After church, lunch, Wal Mart, and AutoZone, I restarted work at around 4:00 PM Sunday.

It turns out that I had to remove every pushrod to insert the new gasket:

Here are the pushrods and the roller rocker assemblies are sitting in roller brush paint pans by the car:

On the pans I wrote whether they came from the front or rear and also noted L and R. All the pushrods seemed to be somewhat differently sized.

By the way, the old gasket was broken around the rear water ports:

You should not be able to see those small slivers of my driveway through the gasket. (I need to learn to take pictures in front of a better background…and get a better camera!!)

New gaskets are installed and end rails buttered up with “sensor safe” high temp RTV:

If you look carefully at the right side of the block, you will see a round opening. That is a port for a distributor. My car has no distributor. Spark is completely controlled by magical computer stuff, and I have three coil packs. This car has an interesting device to block off the port:

This is really the bottom half of a distributor! It has the gear that is turned by the camshaft, and it fits over a hex rod to presumably turn the oil pump. This engine is a great example of old junk engines that work fantastically with modern fuel and spark management systems. Notice the new O-ring from AutoZone. It’s probably not the “dealer correct” part, but I’m sure it’ll do.

By the way, the hex rod is a drastic improvement over my Nova’s distributor. On the bottom of the Nova’s distributor is a fitting that only meshes with the oil pump once every 180 degrees. The hex bit will work once every 60 degrees, and it’s much more likely that the hex bit will fudge itself into position than with my Nova’s fitting.

Here’s that piece in the block with its own distributor hold down clip.

Fast forward to 12:30 AM, and the engine is complete:

Yay! Two solid days of work finally done!!

I started the car up, and the only apparent problem is that the idle seemed rough. The SERVICE ENGINE SOON light blinked. This means that the engine needs service soon to prevent damage. I shut it off and fiddled with stuff, and I think the #2 spark plug wire was loose. I unplugged and re-seated all 6 spark plug wires. It ran great after I started it up. The SERVICE ENGINE SOON light was on again, but it wasn’t blinking. It was late, so I didn’t run the engine for long or drive anywhere, but I think the SES light may shut itself off after several seconds of running provided that something else isn’t wrong.

So after around 19 hours of work, I am probably done with this intake manifold gasket replacement. Man, this is one job I hope to never repeat. The nice thing is that if I ever do it again, I can probably get it done in a day.

UPDATE: The SES light was a hoax. Someone helped me clear out a code on the car’s comptuer the next day, and the light never came on again. All I can guess is that the computer got flummoxed by all its sensors being disconnected and moved over the past two days.