Sewer Line Fix

I am so lucky. We had an expensive sewer malfunction last week, and it’s fixed at no cost to me.

A little background. When we bought this house, the sellers neglected to disclose a few things. One neglected disclosure were known problem with the sewer line. Five days after moving in, our house’s entire sewer system backed up. It did it again a few weeks later. I did a little investigation and found that the previous owners called local plumbing outfits several times to get the line cleared out. And the previous owners even admitted that they regularly put root kill down the drain. Hmmm, repeated cleanouts and root kill, but you think there is no disclosable problem?

Fast forward to two Wednesdays ago, around 18 months since the last sewer line cleanout. I ran the washing machine late at night. While it drained, sewer backed up into our master shower. (The master shower has the lowest drain in the house, so it’s the first to back up.) I went outside and checked our sewer line cleanout. When I pulled off the cap, the clean out erupted with several gallons of sewer water. Eww! Fortunately it was mostly gray water from the washing machine.

The bad thing is that the water level in the sewer cleanout took all night to go down, suggesting a large blockage somewhere in the line.

I got a plumber to my house by 10:00 AM the following morning. He was a referral of a plumber neighbor who is retiring. This guy only does cleanouts, so he has no vested interest in selling me unnecessary fixes (such as a new sewer line).

He spent about an hour with his power auger and used two different blades. When his auger line reached around 55 to 60 feet, it abruptly bound against something. When he retracted his auger line the second time, while using a smaller blade, he recovered mud. This only means one thing: the line has broken and he’s pulling against surrounding dirt.

My heart sunk. A broken line is major bucks to fix. It’s even more expensive at my house because the sewer line has to go really deep against a slight uphill, it’s in the back yard, it’s around 50 feet long, and it crosses a gas line.

But we had a glimmer of hope. The plumber took his line and stretched it along where he thinks the plumbing goes. This line easily stretches into the utility easement. This guy is from Richardson, which does not repair private sewer lines in the easement. The plumber recommended I call Dallas to check their policy.

Fortunately, Dallas does fix sewer lines in the easement! So as long as the problem is in the easement, I don’t pay a cent.

I called Dallas’s 311 service to report a sewage backup. The Dallas Water Utilities truck was at my house in 20 minutes. (It was 12:30 PM by this time.)

Using their own augers and a city drain cleanout truck, the DWU crew confirmed blockages both in my pipe and in the city main. By triangulating, the figured that the problem is well within the 15 foot city easement.

The crew traced my sewer line in a novel way. One guy stuck a large snake in the line, and another guy listened for the whooshing noises the snake made while passing through the line. These noises come clearly even through all those feet of soil. I marked out the line’s location with small marker flags I had sitting around.

The crew also tried other drain clearing techniques, including two different high pressure water jets. Nothing cleared it up. During a re-augering, their auger line snapped in two.

By around 5:30 PM, DWU had another crew at my place to dig out the line in the city’s easement. Unfortunately for my neighbor, that’s on their side of my back fence. (I have no alley.) To make matters worse, these neighbors had just bought this house. Their contract closed about a week before this incident. Fortunately, they were already planning on ripping out some overgrown flower beds that were in the way, so this wasn’t a loss for them. We told them about our “new resident” sewer incident and figured it just must be how people are welcomed to this neighborhood!

This second screw used a sonar device to re-trace the sewer line. It turns out that the prior method of mapping the line was not totally accurate. The sonar retrace had the line about 5 feet from where the previous crew though it was.

I had to leave the house in the afternoon and did not get back until that evening. When I returned, the DWU guys had already fixed everything. My sewer line makes a 90° bend and dumps into the top of the Dallas sewer line. This 90° bend is what broke. Apparently tree roots from an long-gone hackberry penetrated the line. Not only did the tree roots pulverize the bend, they also got into the Dallas sewer line. That explains why Dallas found blockages in both my line and the city line.

The DWU techs fixed everything with press-on PVC fittings.

I got a free sewer line camera inspection out of the deal. It turns out that my sewer line is clay, and it’s in good condition up to the city sewer line. So there go my fears of having to replace that line someday. And that camera inspection is normally at least $250.

It’s now a week and a half later, and the sewer is working fine. I dodged a costly bullet. What a relief!

The only gripe is that Dallas had to put a new lateral cleanout on the neighbor’s side of the fence. But I can’t blame them. It would have been a hassle for them to dig another 10 foot deep hole on my of the yard just for the cleanout. Fortunately, the cleanout is right by the fence.

Replaced My Water Heater

Yesterday, my father-in-law and I spent 12½ hours replacing my water heater.

Our water heater was old. My house’s previous owners did not report changing the water heater on their house condition form. Given their move in date and the apparent date code on the water heater, it was at least 14 years old.

It was showing its age. It couldn’t keep up with a 10 minute shower using a 2.5 gallon per minute shower head. I figure that the dip tube may have gone out or the heat transfer was exceptionally poor.

Fortunately this old heater had not leaked yet.

Here is that old piece of garbage:

In a recent article, Consumer Reports cut open several water heaters and found that, in general, the longer the warranty term, the higher quality the water heater. For gas heaters, a longer warranty means “bigger burners and better heat transfer for faster water heating, along with more anode material and thicker insulation.” The width of our old heater suggests that it may have just been a 6 or 9 year warranty version, so it was probably on borrowed time before we moved in.

Not only is this heater “old and busted,” whoever installed it was a complete moron. Look carefully at the hot water connection:

This is where the installer sweat soldered a ¾” pipe into a ¾” female threaded adapter. The excess solder sitting around the place makes it look like the soldering happened after the adapter was screwed in. The same thing happened on the cold water line. If this is the case, then the nipples that this female copper piece screws into also got extremely hot. What’s on the other side of the nipple on the cold water inlet? The plastic dip tube. What happens to plastic dip tubes when they get extremely lot? Premature failure. So this water heater could have been “damaged goods” for years.

Back to the story.

On Friday night we pre-purchased a 40 gallon 9 year warranty Whirlpool natural gas water heater from my nearest Lowe’s. Lowe’s did not sell a 12 year warranty 40 gallon natural gas water heater.

Side note: of all the water heaters Consumer Reports tested, the only oddity it found was with the Whirlpool 40 gallon ones. CR reported that the 40 gallon 9 and 12 year water heaters’ internal stuff was identical, suggesting you don’t get a better heater by buying the Whirlpool 12 year unit.

On Saturday morning I stopped by a Home Depot and found that an equivalent water heater is $40 cheaper. Lowe’s refused to price match—even though the product was equivalent, it wasn’t the same brand—so I canceled my Lowe’s order. In the end I got a 12 year warranty 40 gallon GE water heater for only $21 more than Lowe’s 9 year version.

I feel better about the GE water heater anyway. Unlike Whirlpool, GE actually mentions water heaters on its site, suggesting they want to be associated with their product. The GE may really be a Rheem unit, the same brand that I have right now.

Getting the water heater was a fiasco. My father-in-law and I had to go to two Home Depots before we found the one I needed. Then when we got there, we spent about an hour figuring out the right parts to hook up a drain line to my drain pan. More on that later.

Here I am wheeling the new heater into the house:

It’s “ Superior ”. Oooh, aaah.

Next we drained the old heater:

This was way fun. I drained this water heater over a year ago without a problem. This time the heater would not drain even though I had hot water valves open in the adjacent bathroom. If I opened the water heater’s cold water inlet valve, the pressure would force water through the hose just fine. But when I shut off the cold water valve, it quit flowing. I even drained the entire house water system and reopened the cold water inlet. That didn’t work. I finally messed with the temperature and pressure (T&P) release valve. It came apart, allowing air to enter the tank and defeating the vacuum. Eureka ! 10 minutes later and I have an empty water heater.

It turns out that there may have been a check ball in the hot water nipple. That would prevent hot water from back-flowing into the heater.

Here’s the T&P valve ripped apart with its guts off to the left:

Next we cut the copper lines on top and disconnected the gas line:

The water heater wheeled out effortlessly with a dolly. Here’s the aftermath:

That’s the T&P drain line to the right. The chimney was taken down and put to the left.

The floor was a mess!

All that gray stuff is dust. Knowing I wouldn’t have access to this area again, I thoroughly vacuumed the floor and wall.

Next I cut off the 90° bend from the hot water line and the valve from the cold water line:

Then I prepped these lines with some fine sandpaper and flux and sweat soldered ¾” copper to male adapters:

Look carefully and you can see where capillary action pulled the solder through the fitting. They show up as those bright spots on the seam where the supply pipe bottoms out in the fitting.

Even though I only had a propane torch, the sweat soldering went fine. It just took a little while to heat up the pipe.

Here are some more views of the sweat solders:

This is the bottom of one of the fittings.

This is the bottom of the other fitting. You can barely make out where my sanding ended and where solder pooled up.

The pipes just goes to a 90 degree fitting and then drops down through the wall to connect to other pipes in the crawl space. It’s not secured very well.

Whoever re-plumbed the house 20 or so years ago did a mediocre job on the plumbing. That’s why I had such a fun time with my shower a few weeks ago.

This may not have been apparent in the earlier picture, but the flooring under the heater was warped. I think that the pre-1991 water heater back could have had a huge water leak. Fortunately we had extra 12×1 lumber in the garage, apparently an old closet shelf. After a few measurements and cuts with a circular saw, we have a makeshift, semi-level floor:

A reasonably level floor was important. These days you need to put a pan below your water heater. That’s a smart thing: if the heater has a small leak, you have something to contain and carry away the water instead of damaging your house. The pan is made out of aluminum, and the water heater’s weight may have bent the pan pretty badly had I put it directly on the warped floor.

Next we threw a new valve on the gas line:

Remember the T&P relief valve line? That line is ¾” copper that runs to the outside. I wanted to use that line for the pan drain, with the T&P valve of the new heater just draining into the pan. (This is apparently standard now.) The drain pan came with a 1” male PCV adapter like this: 1" Male Adapter SCH-40It also included a large rubber washer and large metal nut. The drain pan has a cutout that the threaded end of this PCV part fits through, and the rubber washer and nut tighten against the cutout to make a water-tight connection.

As mentioned earlier, my father-in-law and I spent about an hour at the Home Depot scratching our heads trying to figure out how to connect the drain pan to this ¾” copper line. It wasn’t easy because we had to go from PCV to copper and also do a sudden 90 degree turn into this line, and it all had to be done in a very short distance. The best that Home Depot staff could recommend was some kind of compression fitting that they didn’t carry. Eventually we stumbled across this solution, which worked very well:

What you see is, from bottom to top, is the stub of the T&P valve drain line (I cut it off about 2” above the floor), a 90° street ¾” copper fitting, and a 1” female threaded to ¾” female sweat copper reducer. We also found a piece that’s like the PCV adapter pictured above but without the long, smooth part to the left of the threads. This helped us with water heater clearance. Here’s a picture of the final assembly:

I thought we would pretty things up a bit and cover holes on the wall with flanges:

This can prevent bugs from getting inside.

Unfortunately I didn’t take pictures for the next few scenes. We put the drain pan in place and then got the water heater situated. Manhandling the water heater into the closet was an adventure. The closet opening was only 2” wider than the water heater, and we had to lift the unit up high enough to clear the pan. Fortunately the water heater was shipped on a cardboard base that was approximately the same height as the drain pan. We slid the heater on the base up to the drain pan and carefully rocked and rotated it up and over into the pan. It took about 15 minutes for us to figure this out and do it. Once the heater was in the pan, further positioning was easy.

Given how difficult that was, I am very glad we chose against a 50 gallon water heater. We almost thought about doing it. The 50 gallon unit was only ¼” narrower than the closet and taller.

Here’s a later picture with the heater hooked up to the water lines:

I put 600 PSI forged brass ball valves on top of the dielectric nipples. Then I used male-to-male couplers to hook up those flexible copper lines that run from the house plumbing to the water heater. Man, those flexible lines make me nervous. Instinctually, flexible stuff shouldn’t be on a critical part of the house’s plumbing!

Notice a problem with the above picture? Hint: where’s the chimney gonna go?

Oh, no! The hot water line blocks the chimney! If that’s not bad enough, we also discovered that the new water heater’s chimney is not in the same position as the old heater’s chimney. Another Home Depot trip!

An hour and a half later, I cut the hot water pipe back and installed a new male threaded fitting:

This clears the chimney great. That’s a wet rag below the pipe. It insulates the heater from my torch and catches solder.

The new chimney fits perfectly:

We made sure the new chimney is the same ultimate height as the old one. The old chimney was a 5’ piece and a 3’ piece. The new chimney is two 3’ sections and two 1’ flexible sections. The old water heater was 3½” shorter than the new one, but the bends in those two 1’ flexible sections took out about 2”, so it was close enough.

I also installed a long copper pipe from the T&P relief valve to the drain pan:

Take a closer look at the gas valve on the above picture. Notice how close it is to the heater? The flexible gas hose won’t fit. So when we went back to Home Depot, we got a 90 degree black steel ½” elbow. Now the valve mostly faces up:

We cranked the black steel pretty tight and used plenty of pipe dope.

Everything’s ready for action!

We thought we were done, but we found several small leaks in the brass fittings. I cranked down those fittings tighter than I thought brass should be cranked. With a 12” adjustable wrench, I was really pulling hard at one point. But they still leaked. A quick call to a contractor in Oregon (a member of my Nova listserv) cleared it up. I wrapped one layer of Teflon tape around all the fittings, but he says I should have used 3-4 layers. All my life I had just wrapped one layer of Teflon around fittings. Until now the only Teflon I had really ever used was for fittings on my old Chevrolet Nova’s cooling system, which at most had 16 PSI of pressure. Municipal water pressure is a few multiples of that.

I took all the fittings off, re-taped them with 4 layers of Teflon, and put the system back together. I ended up with one very slow leak, and I corrected that leak with a little more tightening. Here are the fittings after the re-Tefloning:

Next we turned on the gas and leak tested with our noses and with soapy water. We found no leaks.

Next I lit the heater. I had to hold down the red pilot button for a while to let gas flow through the line. The pilot lit perfectly. Here is a picture of the flames taken through the peep hole:

The red hot part is probably the ceramic part around the igniter. I kept the camera’s shutter open for 0.6 seconds to get this.

After we got it lit and let the burner fire up, we heard tapping sounds and noticed an orangish flame. The manual explained it: cold water entering the heater caused condensation. The orange flame and tapping was from water drops falling onto the burner. The tapping stopped within 10 minutes.

This water heater’s dielectric nipples seem cheap:

Inside this is a little rubber flap and no moving parts. Contrast this to my previous heater which completely blocked back-flowing; its nipples may have had a check ball. Already I can feel that the cold water inlet line gets hot as the hot water naturally migrates out. Hopefully this won’t cause too much heat loss.

Other than that issue, I am satisfied with the new water heater. I didn’t have to repeatedly adjust the faucets during today’s shower. It also runs a lot quieter than the previous one. Hopefully this new unit will cut down on our gas bills.

I am pleased to report that I am typing this blog entry a full trouble-free day after the installation.

I am not sure whether I need to correct this later, but the heater leans just slightly:

This picture exaggerates the lean. I will probably correct this with some wood or plastic shims.

One final point: note carefully my wording. Not once did I type “hot water heater.” Water heaters heat cold water, not hot water. It would be technically correct to say “cold water heater,” but I just say “water heater.”

UPDATE: We spent $513.12 on this whole heater replacement. That is more than $300 less than a quoted replacement price, and we got a much better water heater out of the deal.

Master bathroom shower adventure

A few days ago, I had this bright idea that I would replace the shower arm and flange in my master shower. My master shower is really small, and its shower arm is a whopping 9” long.

I tried to unscrew the shower arm, but it wouldn’t budge. After a lot of straining, I finally got some movement, and then I got that sickening feeling of “something turning not for the right reason.”

It turns out that I separated the 90° piece from the copper pipe! In the process of getting the arm out, I also broke some tile. (I stupidly believed that if I yanked hard enough, the surrounding tile would neatly come off. NOT!)

The enlarged opening, with a mangled copper pipe behind it:

The 90° piece that’s not supposed to come off:

This is not even the correct piece for showers. The correct piece would have bolted up to a piece of wood on the back, making it impossible for it to have twisted the supply line like this.

This is bad. Now I have to take apart some of the shower wall.

Fast forward to today.

I start out with a hole in my shower wall:

I used a Dremel with a cut off wheel to remove the grout between that tile and the adjacent tiles. Here’s the Dremel with the cut off wheel installed:

This was just the standard, fiberglass-reinforced metal cutting wheel.

I went through 1½ of those wheels to remove the grout. Here’s a detail shot:

(I love 5 megapixels! This shot was taken at a distance.)

I tried cutting through the drywall behind the tile with a hacksaw blade. I couldn’t get good leverage or speed, so it was plodding slowly and sloppily. A trip to Home Depot and a compact hacksaw purchase saved me:

With this thing I just sailed through the drywall.

Hallelujah, the tile and drywall are out, and better yet there is drywall behind the drywall! I have a surface to glue my drywall square to when I am done. Take note of the mangled pipe:

Here’s the drywall/tile square:

A few minutes later I hacksawed the mangled piece off the end of the supply line:

Here it is:

Uh, oh, notice the not rounded shape? Argh!

I spent the next several minutes coaxing the supply line to a rounded shape so that I could fit a coupling over it. After massaging with some channel lock pliers and a Dremel bit and hammering the coupling on with the pliers, I finally got the coupling over the supply line.

Notice in a previous picture how there is a large wood piece behind the supply line? I measured that there is a ¾” gap between this wood piece and the supply line. Luckily, I had ¾” thick wood in the garage. A few minutes later and this is what I ended up with:

The two wood screws on the top were only about 1” long. That’s all I had. That left a scant ¼” of screw length to bite into that other wood piece, so I had to countersink their holes just over ¼”. That way these wood screws could bit and secure themselves in the backing wood.

Before I went too much further, I placed the tile back into position and put a copper pipe through to line up where the piping needs to end up:

This let me put some crosshatches where things should end up:

You’re looking through the tile to that wood piece I bolted on.

A few minutes later I sweat soldered the coupler to the supply line:

Notice the burn marks? I aimed a propane torch at the pipe while soldering. The fire wandered a bit.

Before making the final solder, I need to test fit everything:

I somehow managed to make the pipe end up just a hair to the right of where it used to be. In the end it still worked out OK. See the washers behind the supply line? In the process of mangling the supply line and forcing the coupler on, I bent the line a hair so that it was slightly angled away from me. I used the washers to force the line to face parallel to the wall so that I could slip the 90 degree fitting in.

By the way, I had already soldered a short length of copper pipe to the 90 degree fitting that the shower arm is screwed into.

Now I sweat solder the last joint, the top of the coupler:

The wood is even more scorched! The top left side burned on its own at one point. I was able to just blow it out.

Now it’s time for a leak test:

Passed with flying colors! (The only thing that leaked was the pipe plug itself. I didn’t screw it in tightly enough.) Oh, yeah, notice that the 90 degree fitting is now screwed into the wood piece.

Liquid Nails will hold the tile/drywall square once I put it back on:

Yay!

Fixing the broken tiles with latex caulk:

It’s not a perfect cosmetic fix, but it will keep the area dry at least.

Doesn’t look that bad:

My very messy grout job:

Here’s the whole thing all cleaned up with a new showerhead:

Yay!

I was going to replace the shower arm in the hallway bath, but I changed my mind. That shower arm is not secured to anything, so I would probably be stuck with the same situation if I mess with it.

Sodded the Back Yard

For about 12 grueling hours, two in-laws, my wife, and I sodded the back yard with Palmetto St. Augustine grass.

At 7:45 AM Miller Grass delivered six pallets of sod. Each pallet is 63 square yards, or 567 square feet. Six pallets are a whopping 3402 square feet!

Our Palmetto pallets are the rearmost ones on this truck:

Here’s what the yard looked like before we started (click on it for a larger version):

Notice the playground area and other junk on the yard.

Here is a progress check at around 2:00 PM:

Did you notice that the playground area is gone?

As we got through the first pallet, I noticed that it covered disturbingly high percentage of the yard. I freaked out and estimated that I somehow bought 50% more sod than needed.

We took a careful look at this playground area and decided to just rip it out and grass it over. The equipment was decrepit anyway, and the playground area’s mulch was mostly worn out and eaten up. All the junk on the right side of the yard is from this playground area.

Even after making this decision, I was still concerned that we would be left with two unused grass pallets. I called Miller Grass and asked if they would buy back the two pallets, but they were understandably not interested. Sod is like take out food. Once the food is prepared for you and it’s in your possession, you can’t just take it back. Miller Grass referred me to a landscaper who needed two pallets of grass for Sunday. I called the landscaper, and he offered me 50% of my cost for the grass.

Fast forward to 6:30 PM:

We’re done, and better yet we used every last piece of grass! The landscaper didn’t get to buy a thing.

My original plan was to solid sod a third of the yard, checkerboard sod another third (the area already had some grass), and leave the rest alone (the remainder had healthy St. Augustine or was the play area). Well, it turns out that after sodding the playground area, we had exactly enough grass to solid sod the entire yard, not including the area with healthy St. Augustine. What incredible luck! For a price that I thought would give me enough to halfway finish the yard–and leave a trashy “playground” in the middle of it–I now have a stunning back yard. The difference between before and after is astounding!

The thing that I am most proud of is that I personally unloaded at least a third of the grass from the pallets into the back yard. It was one of the most difficult jobs I have ever done, and I am exhausted. But considering that 3½ weeks ago I was in the emergency room after a bad crash, this is a major accomplishment.

By the way, that grass stunk of cow manure.